Just a little update on the progress from the past 6 months or so. After about 2 months the new fuel pump failed on me. Was just driving along and then slowly started to loose power until the point where foot was flat to the floor and just nothing. Was put on a tow truck and straight the to workshop. Was lucky to catch the mechanic in there on a Sunday afternoon. Fuel pump was ordered and replaced couple days later. Got it back and it was all good. That pump last about 3 months until it started surging on me. Got a video of the fuel flow will upload if I can find it. After the second fuel pump failing I took it to another workshop to get the problem sorted out. So fuel pump was replaced and car was on the dyno getting retuned and the timing chain skipped a tooth. So while we had things off to do the timing chain I decided it would be a good time to throw in some valve springs and billet oil pump gear. Got that done and back on the dyno it went to finish up the tune. Was driving past the mechanics and thought I would stop in to see how it was all going. Car was pretty much done just needed to take it for a test drive then it was all mine. So I was standing there talking to the mechanic and the radiator decided it had had enough and decided to let go, just sitting there idling and it let go. It was at that point in time me and the mechanic both looked at each other and said what else can go wrong with this car. It was just one drama after another. After replacing the radiator I was given the car back with it still making roughly 350kw. Couple months later I start hearing another noise, like a really faint grinding noise. Which slowly turned into a not so faint grinding noise and then the high pitch whistle noise. After about a month or so I decided to actually confirm my suspicion and took my intake off to find there was that much play in the turbo it just wasn't funny. So back we went to get a new turbo. Gtx3582r order and arrived the next week. Dropped car of while I went to work for a week. Called him up the the day before I got home to see how everything was going and turbo was on and car made 383kw but it started to miss and break down a little on the top end so he suspected coil pack. Water pump was also very noisy so both were replace. Went in when I got home the next day and first thing he said when I walk in is I got good news and bad news. Which is probably the last thing I wanted to hear. Good news, car made 399.5kw and the bad news.... Clutch was slipping. So power was taken out till it stopped slipping so it's sitting at roughly 360kw till the new clutch goes in. So plans for the car next year are a new clutch, surge tank and put some e85 in it and see what else we can blow up!! Sent from my iPhone using Tapatalk